By pre-connecting fixed hydraulics and electrics to the source, the 340K has removed the need for separate console lifting – reducing rig up times.
The 340K's 15" stroke offers more flexibility than the standard 10" stroke.
Exit to the unit using stairs and ladders offers a safer access solution.
The 340K Units can be configured to suit P&A, Snubbing and Workover operations.
| Pull Capacity | Push Capacity | Stroke | Thru-bore | Main Winch Pull Capacity | CB Winch Pull Capacity | Rotary (High) | Rotary (Low) |
|---|---|---|---|---|---|---|---|
| 340,000 Lbs | 170,000 Lbs | 15 ft | 21.5" | 11,000 Lbs | 5,500 Lbs | 80 RPM @ 12,000 ft-lbs | 40 RPM @ 24,000 ft-lbs |
A new standard in well operation performance
High pulling capacity. Large through bore. Ideal for well abandonment.
The next level of unit engineering and design
Maximum capacity and performance for well abandonment
Safely meeting the pressurized well challenge
Electric power for reduced emmissions
Two gas platforms in the Celtic Sea had reached the end of their economic life. WellGear mobilised a 340k and a 460k Unit to plug and abandon their wells.
When a blocked completion prevented a well from being killed, the WG003 HWO was mobilised to pull the completion live and then kill the well.