The unit’s Modular, pinned connection design ensures rapid rig up and rig downtimes. The 15" strike increases the efficiency and flexibility of the unit compared to the traditional 10" stroke.
The bespoke blowout preventer (BOP) substructure is capable of handling BOP's up to 21-1/4" with the ability to change them while the unit is in situ.
| Pull Capacity | Stroke | Thru-bore | Main Winch Pull Capacity | CB Winch Pull Capacity |
|---|---|---|---|---|
| 600,000 Lbs | 15 ft | 27.5" | 27,500 Lbs | 5,500 Lbs |
A new standard in well operation performance
High pulling capacity. Large through bore. Ideal for well abandonment.
The next level of unit engineering and design
Maximum capacity and performance for well abandonment
Safely meeting the pressurized well challenge
Electric power for reduced emmissions
Two gas platforms in the Celtic Sea had reached the end of their economic life. WellGear mobilised a 340k and a 460k Unit to plug and abandon their wells.
When a blocked completion prevented a well from being killed, the WG003 HWO was mobilised to pull the completion live and then kill the well.